Ok here is a little info on what happened on that run....
The engine on the dragster wound to high C shortly after the launch, which sent the car's PSI, overdriven by about 80%, to 20,000 rpm. At that point, centrifugal forces seperated the large cast - aluminium male and female rotors into a hundred pieces, and the shards took the supercharger case with them. Particularly troubling to NHRA officials was what happened to the blower bag surrounding the unit: it was gone. According to Drazy, the Lenco car's overspeed condition was not the sole cause of the disintergration; over - speeds have happened in the past on PSI's, without rotor failure. In the case of the Lenco car, the supercharger had been subjected to a number of backfires in the months prior to the Phoenix race, which weakend the strength of what Drazy subsequently learned was an already brittle casting. When the rotors were momentarily spun to 20,000 rpm, they seperated along stress cracks developed during the backfires.
I'll type up the full article later on after I've rested. I just got home from work and found this write up in one of my zines.
Regards,
Mike